I have a 4 hp 4 stroke built in Dec 2008. Until recently ran well. Fuel bulb from aux tank rotted and I believe got some debris past the filters. Carb was removed, cleaned and re-installed. All fuel lines cleaned and fuel filters changed. Fired right up and ran in the barrel for about 10 minutes from the internal tank then flooding began again. I have reviewed other forums and this seems to be a common issue with everyone guessing on a solution but no final conclusion. I see nothing causing the needle or float to be the issue. Is there a check valve in the fuel pump that could be stuck allowing too much pressure? These carbs seem pretty simple and common but this has me baffled.
Any help would be welcome.
Thank you.
Walt Drechsler
Any help would be welcome.
Thank you.
Walt Drechsler
Comment